Sign in   |  Join   |  Help
Untitled Page

ARCHIVED FORUM -- March 2012 to February 2022
READ ONLY FORUM

This is the second Archived Forum which was active between 1st March 2012 and 23rd February 2022

 

Beogram 6500 fuse constantly blowing

rated by 0 users
This post has 46 Replies | 2 Followers

Steve
Not Ranked
Cape Town
Posts 73
OFFLINE
Bronze Member
Steve Posted: Tue, Jul 26 2016 7:15 PM

Hi 

 

I've recently moved house - and my Beogram 6500 has blown two fuses. It was working when I moved in, but every night when I come home the turntable won't power up and fuse blown. The first time I replaced fuse it played fine all evening.. but then tonight I come home and the new fuse is gone. Is this a power / surge issue in my apartment block.. or something problematic with the electronics?

 

any advice appreciated!

steve

Beobuddy
Top 25 Contributor
Utrecht, The Netherlands
Posts 3,972
OFFLINE
Founder
Beobuddy replied on Tue, Aug 2 2016 12:24 PM

Bad solderjoint at the large 1000uF next to the fuse. 

Or the cap itself is faulty. I replace them always. 

Dillen
Top 10 Contributor
Copenhagen / Denmark
Posts 13,191
OFFLINE
Founder
Moderator
Dillen replied on Wed, Aug 3 2016 7:36 AM

I agree.
Or someone with very little electronic knowledge made the mistake of fitting Schottky diodes as rectifiers.
I have seen this twice now (Eh???)

Martin

Menahem Yachad
Top 75 Contributor
Jerusalem, Israel
Posts 1,249
OFFLINE
Bronze Member

Hi Martin

 

Just curious - why this comment? 

"Or someone with very little electronic knowledge made the mistake of fitting Schottky diodes as rectifiers."

Nothing personal - just the technical reasons.

 

Today, Schottky diodes have become the defacto first-choice for rectifiers in power supplies.

In fact, their first widescale applications in the 1990's, were for the secondary Low-voltage stages of all VCR power supplies.

Today you will hardly see a power supply without Schottky diodes.

 

Of course, they are not as forgiving as a regular diode, and the tech should be over-generous in selecting a suitable current rating.

 

Menahem


Beobuddy
Top 25 Contributor
Utrecht, The Netherlands
Posts 3,972
OFFLINE
Founder
Beobuddy replied on Fri, Aug 12 2016 11:15 AM

Maybe for the exact reasons you've just mentioned?

Schottky diodes are overkill for an old fasion powersupply as used in the BG6500.  Using the Schottky's in combination with the original used Roederstein capacitor, will result inevitable cease of it. The rush-in current will be to high for it and will result in a shortend cap.

The voltage-drop is much lower and results in a higher voltage at the entrance of the rest of the powersupply.

So, juts fiitting some ordinairy older 1N400x or 1N540x would be fine.

If you would use these more modern Schottky diodes into older devices like the BM900/1000 etc, then you will end up with fried output transistors.

So, I think you (generally speaking) need to think twice about where you are going to use these parts and if they are suited for the job, instead of just thinking that newer more modern parts are always better.

Menahem Yachad
Top 75 Contributor
Jerusalem, Israel
Posts 1,249
OFFLINE
Bronze Member

Thanks for your reply, but personal experience proves otherwise.

Firstly, if a tech is going to change the diodes, then smartness suggests that he also upgrades the filter cap as well. Modern filter caps have a much better capability to handle the inrush than the older ones, so THAT is not a problem. If one is going to do the job, then do it completely, not just a half-job.

Secondly, the extra voltage is NOT a problem. ALL BeoMachines have a voltage regulator after the bridge, and an extra volt on the regulator input is NOT going to make any difference at all. Not only that, but the smoother waveform of a Schottky vs a 1N400x, reduces the input stress on the regulator.

Fried output Transistors? Perhaps on some isolated ancient machines, but not on anything made after 1975.

My own BG3400 was upgraded with Schottky's well over 10 years ago. I haven't had to open it since.

Ditto my BeoGram 4000.

Martin mentioned the BG6500. My own BG4500 (the same as the BG6500), was upgraded with Schottky's on EXACTLY that circuit over 10 years ago, during a complete overhaul and upgrade. I have NEVER had a minute's problem with it.

I have done the same overhaul on many other BeoGrams of the same series, and am in regular contact with the owners - none has ever had a problem.

I intend to upgrade the 2 round rectifiers in my recently-acquired and previously-dead BM4400 with 4 Schottky's wired together, with absolute confidence that there will be no unfortunate side-effects, ever. I'll keep you posted honestly, if I'm subsequently proved a fool.

The only caveat which I can issue is stay away from cheap Chinese Schottky's - you're asking for trouble. Anyone who is investing the effort to do such an upgrade should not be looking anywhere else than Vishay's diodes. Yes, they cost more, but they last n times longer than the Chinese look-alikes.

Of course, I do not willy-nilly change components - I make a very  comprehensive examination of what the circuits require, and match the new components to those requirements.

There may be some ancient BeoMachines which will experience cardiac arrest with Schottky's, however, to make a blanket condemnation both of the installer's intelligence level and the equipment, simply does not suit the integrity of the people on this forum.

 

Martin mentioned in another thread how important the right belt is for the BG1000 and other round-belt turntables.

He said perfectly intelligent things about the cheap Chinese look-alikes.

So it is with Schottky diodes. There is Vishay, and there is junk. Do not expect junk to last - in fact, expect it to damage your BeoMachine.

But do not write off all Schottky's, just because the Chinese junk damaged the machine.

 

Menahem

Dillen
Top 10 Contributor
Copenhagen / Denmark
Posts 13,191
OFFLINE
Founder
Moderator
Dillen replied on Fri, Aug 12 2016 2:35 PM

Conventional diodes are more forgiving, yes, - and far more reliable.
I've seen two cases of the above Beogram types with shorted and/or physically exploded Schottky diodes and in both
cases I could tell, that they weren't factory fitted.
In both cases the diodes were the only culprits, and fitting conventional (I like to use 1N4002-1N4006) diodes
brought back normal function.
You can design circuits to use Schottky diodes but replacing conventional diodes with Schottkys in an existing circuit is pointless.
Waste of time and money in the best of cases, and in rectifier positions it would be asking for trouble and unstability.
Been there, done it, saw it twice, got the T-shirt.
Paid for it too.

I never saw a blown output stage transistor because of a Schottky-based rectifier, but it sure is possible.
And it has nothing to do with the circuit being produced pre- or post-1975 (where did that year come from anyways?),
10 ohms year 1960 is still 10 ohms year 2016. 10 Volts are also still 10 Volts.

But how come that now, when Schottky diodes are available, we are still using conventional diodes?

Schottky barrier diodes have a lower turn-on voltage and faster recovery time.
They are generally "faster".
There are some places, where a Schottky diode is preferred but there are many more applications, where it's
not recommended to use Schottky diodes.
- And for a number of reasons;

They have a higher reverse leak current.
They don't handle power particularly good - and if put to work with higher currents they lose their Schottky properties anyways.
They are considerably more temperature dependent.
Their internal capacitance is even more temperature dependent, often to the extent of being quite unpredictable.
They are typically larger.
And they cost a bit more, up to twice the amount of a similar silicon diode, though this is probably mainly of interest in large production.

The temperature dependency is a problem, which together with the higher reverse leak current and the almost ever
changing internal capacitance can cause a thermal runaway, which typically ends with the diode shorting - or
even exploding, depending on the current flow in the given application.
(The diode doesn't even have to work in a high voltage circuit to do this).
In other words; In areas where temperature changes are to be expected (f.e. power supplies and amplifiers), Schottky
diodes should only be used with the utmost care.
Any place a conventional silicone diode can be used instead of a Schottky, it should - to make a much more reliable circuit.

In existing circuits, like power supplies, where the first component following the rectifier and
filter capacitor is a voltage regulator, the lower forward voltage drop of the Schottky diodes
will make the input voltage to the regulator higher, which again increases the voltage drop that the
regulator has to make to output its nominated voltage. This puts a higher load
on the regulator and it will have to dissipate more energy (it will run warmer). The diodes will then of
course dissipate less but the total heat dissipation will be the same and the heat is often better distributed at the
four diodes (that rarely needs additional cooling anyways).
If you design a conventional power supply circuit from scratch, you can choose a transformer that outputs a lower
voltage but there's really no point in doing so if only to spend money on more expensive rectifier diodes
(- that won't do the job any better - and give unstability with changing temperature).
If you at the same time put a low-ESR filter capacitor after the rectifier, keeping the lower forward
voltage drop of the Schottky diodes in mind, then the transformer (and the fuse!) will see a higher
rush-in current.
And so will of course the diodes...
In most cases, the rush-in current is not a problem for the capacitor but potentially for all the other
components upstream, that has to carry it.
- And there's really no need for either a low.-ESR filter capacitor nor "fast" rectifier diodes in the Beogram power supply (100Hz).

High frequency circuits are where the Schottky diodes usually do their best and where it makes sense
to call in "faster" diodes.
Radio frequency circuits, IF-stages, mixers/frequency changers and the likes.
Transistors used in high frequency switching circuits can also, in some cases, benefit
from a "Schottky clamp" between base and collector. Think of the 74LS TTL logic IC series, where the LS stands
for Low-power Schottky - allowing them to operate at higher frequencies than the standard not-LS types.
Do remember to fit a 100nF capacitor across the supply very near to the IC and preferably directly on top of it - or
the schottky-based circuit will give unpredictable results (!!!!!).

If you design your own circuit, you can design it to use Schottky diodes if you are absolutely sure you
know, what you are doing.
Replacing conventional silicon diodes with Schottky diodes in an existing circuit will
not improve the circuit in any way. Quite contrary if anything.

For 50Hz rectifiers, replacing conventional diodes with Schottky diodes because they are "faster" would
be downright ridiculous.
The good old 1N400x series (and something like 1N5401 in higher current applications) - would be an
excellent choice for rectifier purposes in most stereo/audio applications.

Substituting conventional diodes with Schottky diodes to make circuits run cooler simply doesn't make sense.
Doing it in the name of increased stability is electronics misunderstood. Regardless of the brand.

And this is by no means meant personal. It's just facts. Wink

- And I don't buy chinese.
Been there too. Laughing

Martin

Menahem Yachad
Top 75 Contributor
Jerusalem, Israel
Posts 1,249
OFFLINE
Bronze Member

All quite correct - no arguments.

But there is always room for well-thought-out exceptions ;-)

 

Test a Vishay 31DQ10 for reverse leakage - let me know what you find.

Initially this was my skepticism "barrier" to investigating Schottky's - I was pleasantly surprised.

As I stated, the tech considering a Schottky upgrade must be over-generous in his choice of current rating - meaning double or triple.

 

The main benefit of using Schottky, is to my ear, better sound with a wider and more dynamic soundstage.

I've A-B'd it, and so I find it.

I mentioned 1975, because that's the approximate year that B&O stopped using the TO-3 2N3055-type low-gain output transistors, and changed the amp circuit design to the TIP141/6 high-gain Darlingtons.

That's where a change to Schottky's will be beneficial and audible - in my experience.

 

Take note that I did NOT (and still do NOT) advocate replacing the large rectangular B80C main 50Hz bridges with Schottky's.

In fact, I've never had reason to replace any B80C bridge in any European machine on which I've worked.

As I mentioned - the round 1A bridges are the components I look at for upgrades - and they are generally feeding the IF/RF circuits in BeoMasters.

Wholesale "upgrades" with no forethought is not an upgrade, and may be destructive.

Dillen
Top 10 Contributor
Copenhagen / Denmark
Posts 13,191
OFFLINE
Founder
Moderator
Dillen replied on Fri, Aug 12 2016 3:28 PM

Test any Schottky diode for reverse leakage, put to work with varying temperature.
And test their Schottky properties when handling current. (Save your time - there won't be any Laughing).
Schottky diodes are Schottky diodes.
With their benefits and drawbacks.
It's in their nature.

TIP141/TIP146 etc. darlingtons already have an internal diode between E-C so I would hesitate adding a
Schottky clamp here (or put a Schottky diode anywhere else in AF-circuits for that matter).
Seeing as the benefit of Schottky diodes really first becomes evident above several MHz, I really
don't think that there will be any audible difference below 20KHz - let alone if used in the (50Hz) power supply.

No Schottky diodes in power supplies, power amplifiers and AF-circuits.
Keep them away from places where power is handled and where circuits have feedback.
Use them in tuners and particularly in high-speed digital/switching circuits (computers and the likes), that's where they belong.

You are free to do and fit whatever you feel for, it's your machines (and your clients) but I
would never use a Schottky diode where I could use a conventional diode. No exceptions.

We may not agree but electronic facts are electronic facts and
facts ask noone to agree. Laughing

Martin

Beobuddy
Top 25 Contributor
Utrecht, The Netherlands
Posts 3,972
OFFLINE
Founder
Beobuddy replied on Sat, Aug 13 2016 2:25 PM

Most circuits have a regulated power management.

But most, if not all, the output stages have an unregulated powersuply.

I referred to the older amplifers with germanium transistors/output stages. These are fed with selenium rectifiers. The used "diodes" inside regulate the rush-in current. Replacing these with more modern version (e.g.Schottky) diode will result in silent output stages.

Schottky diodes are only neccessary where low drop voltages are required at higher switching supplys (PWM). Frequency's here used are above 30khz.

And As Martin already stated, you're shifting a part of the power dissipation from the diodes to the voltage regulator. And the older regulators are far from efficient.

Ever thought of what happens in a circuit when you switch the power on? That's the moment where the most parts cease and at older used age ,( like e.g. light bulbs). The highest current will be at that moment. All, or most current equipment are suited with special rush-in resistors. To protect the circuits (with used schottky's) diodes behind it.

The main thing is to think what the appropriate needed components are. It's like a chain with it's weakest link.

Menahem Yachad
Top 75 Contributor
Jerusalem, Israel
Posts 1,249
OFFLINE
Bronze Member

On the tube equipment which I restored, I always remove the selenium rectifier and replace with a normal silicon rectifier, and then a series resistor on the B+ line - generally a 100 ohm 10 watt. That has 2 benefits, one - to drop the increased silicon voltage to the required level, and two - to act as an inrush limiter.

The Selenium stinks when it fails, and the small extra effort to change it when the radio is in for its initial work, is well worth it to prevent a subsequent service call. 

Steve
Not Ranked
Cape Town
Posts 73
OFFLINE
Bronze Member
Steve replied on Mon, Aug 15 2016 1:52 AM

Hi gents,

 

thanks for for the feedback. It turned out to be T4 and/or T5 - both BC337 type transistors on PCB1. Power was leaking back to motor during standby. All working 100% again. 

 

Thanks 

Dillen
Top 10 Contributor
Copenhagen / Denmark
Posts 13,191
OFFLINE
Founder
Moderator
Dillen replied on Mon, Aug 15 2016 10:08 AM

That's not the first time we see problems with the BC337 transistors in these decks.

Thanks for telling us your findings!

Martin

kimhav
Top 500 Contributor
Malmo, Sweden
Posts 314
OFFLINE
Bronze Member
kimhav replied on Sun, Jul 5 2020 5:37 PM

Interesting findings here; picked up a BG6500 yesterday which was working before I loaded into the car and when I came home totally dead. Fuse was blown which I replaced and what I can figure out is that the fuse seems to either blow directly when connecting the 230V or when I press the play button. The Power Supply board PCB2, how do one take this out without damaging it since one of the TR's is fitted to the bottom of the Beogram with a heat sink?

Dillen
Top 10 Contributor
Copenhagen / Denmark
Posts 13,191
OFFLINE
Founder
Moderator
Dillen replied on Sun, Jul 5 2020 5:50 PM

The "transistor" (it is in fact a voltage regulator) sits in a socket. The board pulls right up after
you release its holding claw.

This type of filter capacitor (Roederstein) is known to develop shorts.

Martin

kimhav
Top 500 Contributor
Malmo, Sweden
Posts 314
OFFLINE
Bronze Member
kimhav replied on Sun, Jul 5 2020 6:00 PM

Right, taking a closer look now so the regulator is the IC1 7812 and the C3 1000μF is the one you're ref to Martin that most like is the issue here

While looking at the caps they in general looks good; no leakage or any other indications that they're bad but still; if one should pick together a capkit for this BG6500; any recommendation of additional caps to be replaced and as well other components if I'm doing a full overhaul of it?

Dillen
Top 10 Contributor
Copenhagen / Denmark
Posts 13,191
OFFLINE
Founder
Moderator
Dillen replied on Sun, Jul 5 2020 6:09 PM

kimhav:

Right, taking a closer look now so the regulator is the IC1 7812 and the C3 1000μF is the one you're ref to Martin that most like is the issue here

Yes.

kimhav:

While looking at the caps they in general looks good; no leakage or any other indications that they're bad but still; if one should pick together a capkit for this BG6500; any recommendation of additional caps to be replaced and as well other components if I'm doing a full overhaul of it?

No. Just the one
- If it's bad. Check it with an ohmmeter.
You cannot always tell if a component is bad by looking at it.

Martin

kimhav
Top 500 Contributor
Malmo, Sweden
Posts 314
OFFLINE
Bronze Member
kimhav replied on Sun, Jul 5 2020 9:51 PM

Martin you wouldn't know where one could order Vishay 1000uF 40V mounting ring based caps since neither Farnell och TME stocks them.

skolesen
Not Ranked
Hvidovre, Denmark
Posts 34
OFFLINE
Gold Member
kimhav
Top 500 Contributor
Malmo, Sweden
Posts 314
OFFLINE
Bronze Member
kimhav replied on Mon, Jul 6 2020 7:49 AM

Yes I saw that it's possible to get these on eBay but kind of reluctant to get NOS which still could be bad so kind of rather go for Vishay (old Philips) caps (who still makes this mounting ring based cap) or I'll most for Panasonic caps.

Dillen
Top 10 Contributor
Copenhagen / Denmark
Posts 13,191
OFFLINE
Founder
Moderator
Dillen replied on Mon, Jul 6 2020 9:18 AM

The ring is not necessary as long as you use the right holes and solder pads for the positive (center pin) and negative (circumference pins) respectively.
Any standard type (perferably not low-ESR) type will be fine.

Did you confirm that the capacitor is the problem?

Martin

kimhav
Top 500 Contributor
Malmo, Sweden
Posts 314
OFFLINE
Bronze Member
kimhav replied on Mon, Jul 6 2020 7:42 PM

Dillen:
Did you confirm that the capacitor is the problem?

Manage to remove the clip that holds down the regulator and disconnected the power cords going to the RIAA and main PCB. About the capacitor, I would say that it most likely is alright, while I don't have any multimeter to measure the capacitance, it does seems to load and discharge when measuring with high ohm range. Also, checking the power supply the output to PCB2 is 19.3V and the output from the PCB2 is 12.03V. Next I connected the power to the RIAA PCB again to see if the fuse would hold - it did. Next connected the power to the main PCB and pressed the play button - the fuse didn't blow this time and the platter started to spin and the tone arm indicated 33rpm. So suddenly everything seems just fine. Short term: Yay! But, hey what did cause my init problems and why? So open for suggestions here.

 

Menahem Yachad
Top 75 Contributor
Jerusalem, Israel
Posts 1,249
OFFLINE
Bronze Member

I agree that buying old NOS capacitors is akin to taking a chance with "a cat in a sack", regarding reliability.

I have brand-new stock of the EXACT Vishay replacement part MAL212047102E3 , 1000uF 40V 125C, with the ring.

Contact me off-line.

Menahem

kimhav
Top 500 Contributor
Malmo, Sweden
Posts 314
OFFLINE
Bronze Member
kimhav replied on Sun, Jul 12 2020 9:32 PM

@Menahem I'll send you an email on the topic.

kimhav
Top 500 Contributor
Malmo, Sweden
Posts 314
OFFLINE
Bronze Member
kimhav replied on Sun, Jul 12 2020 9:37 PM

@Dillen I did got around to re-connect the BG6500 to the BM6500 today and it worked as a charm but sitll not happy with that it blew some fusses after the 400km journey home to Malmo. It might be nothing or it might be something. But, the idea is still to re-cap the unit.

So for now only thing that I had to replce was the needle which sounds totally rusty but have spare needles so once the switch was done is sounded great again.

Also about the regulator on the PSU-board; how on earth to you re-attach the heat clip again to the bottom of the beogram?

Dillen
Top 10 Contributor
Copenhagen / Denmark
Posts 13,191
OFFLINE
Founder
Moderator
Dillen replied on Mon, Jul 13 2020 6:21 AM

Not easy.
Clip it to the bottom plate before inserting the PCB.
I seem to remember the easiest way is to slide the clip in, little by little, lifting its leading edge with a small screwdriver as it goes over the regulators housing.

Martin

kimhav
Top 500 Contributor
Malmo, Sweden
Posts 314
OFFLINE
Bronze Member
kimhav replied on Sun, Apr 4 2021 7:07 PM

Got around to look into this turntable again after that I finally got around to play couple of records yesterday and after couple of hours it died on me.... blown fuse again. So checked the PCB2 board so checked the 7812 which is alright and replaced C3 (1000u); so have a good 12V out from the board - but still fuse blows and only blows when PCB1 is connected. So beside checking the BC337 and other tips on what to check?

Menahem Yachad
Top 75 Contributor
Jerusalem, Israel
Posts 1,249
OFFLINE
Bronze Member

Looking at this problem as you describe it, this would be my procedure - cheap and quick enough to do, without getting into in-depth troubleshooting..

1. On the PSU PCB, Replace the 4 Si rectifier bridge diodes, with a 1.5A unit - perhaps the 1N5393 or similar.

2. Replace the 12V regulator with a L78S12CV - more robust 2 Amps

Connect a 60W incandescent bulb across the fuse terminals - saves fuses.

If the problem still happens, then disconnect the output of the 12V Regulator from the circuits down the line.

Connect an AMMETER (not a voltmeter) between the 12V Regulator output, and all the other down-line circuits.

The objective is to monitor the Amperage, and when the Bulb illuminates (instead of blowing the fuse), check the Amperage at that EXACT time.

That will tell you where the problem is, and is not.

kimhav
Top 500 Contributor
Malmo, Sweden
Posts 314
OFFLINE
Bronze Member
kimhav replied on Sat, Apr 10 2021 3:21 PM

So finally weekend again and due to the nice weather today the garden got it's fair share of TLC as well today after the winter :-) So moving over to the BG6500. So based on your suggestions Menahem I've replaced the bridge diodes including the 12V regulator; so the PCB2  should be in the clear now based on that I've replaced all of the caps and diodes.

Well, fuse still blows. Right, so started check the diodes on the PCB1 and D1 (IN4002) didn't pass, so this one needs to be replaced as well. So question here why would would cause D1 on PCB1 to go bad; transistor leakage?

Dillen
Top 10 Contributor
Copenhagen / Denmark
Posts 13,191
OFFLINE
Founder
Moderator
Dillen replied on Sat, Apr 10 2021 3:48 PM

Is D1 open or shorted?
Can you take an ohmmeter reading across C2 and another from IC1 pin 9 to ground?

Martin

kimhav
Top 500 Contributor
Malmo, Sweden
Posts 314
OFFLINE
Bronze Member
kimhav replied on Sat, Apr 10 2021 4:19 PM

D1 is open. Measuring C2 (470 uF) gives reading (increasing ohm value) and IC1 pin 9 to ground indicates that it's closed (low ohm reading).

Dillen
Top 10 Contributor
Copenhagen / Denmark
Posts 13,191
OFFLINE
Founder
Moderator
Dillen replied on Sat, Apr 10 2021 4:32 PM

IC1 shorted then, if you're sure about those readings.
That's quite unusual.
Can we see a photo of IC1?

Martin

Dillen
Top 10 Contributor
Copenhagen / Denmark
Posts 13,191
OFFLINE
Founder
Moderator
Dillen replied on Sat, Apr 10 2021 4:34 PM

Could also be that D2 has shorted. Lift one end and put your ohmmeter across it.

Martin

kimhav
Top 500 Contributor
Malmo, Sweden
Posts 314
OFFLINE
Bronze Member
kimhav replied on Sat, Apr 10 2021 5:03 PM

Martin, I misread what you wrote; I measured IC1 PIN1 to general ground. Measuring IC1 pin 9 to IC1 ground and pin 9 to general boards ground it open (and IC1 looks fine) and regarding the diodes:

D1 = 631 and switching polarity gives 1609 instead of OL so it's bad.

D2 = 122k ohm (measured directly over it)

D9 = 630 and switching polarity gives OL so it's good.

 

 

Dillen
Top 10 Contributor
Copenhagen / Denmark
Posts 13,191
OFFLINE
Founder
Moderator
Dillen replied on Sun, Apr 11 2021 7:07 AM

Sounds fine then.
Sure you fit the correct type and rating of fuse?
Is a RIAA fitted in your Beogram?

Martin

kimhav
Top 500 Contributor
Malmo, Sweden
Posts 314
OFFLINE
Bronze Member
kimhav replied on Sun, Apr 11 2021 8:30 AM

Yes, using slow blow 500 mA fuse so that should be fine as well. But, for now I'll just need to fix that bad D1 diode (any idea was this one gone bad?) and going  to check the mentioned transistors above also. Yes, the 6500 has a RIAA fitted, but as mentioned the fuse blows only if the PCB1 board is connected to PCB2. Haven't removed PCB1 board one yet from the turntable but going to do this today to do the work.

kimhav
Top 500 Contributor
Malmo, Sweden
Posts 314
OFFLINE
Bronze Member
kimhav replied on Sun, Apr 11 2021 12:31 PM

Here is the full PBC1-board which in general looks fine:

But there are two areas on the boards which shows signs of heat; first area is the resistor cluster R38 - R45 in the corner area:

Including around R3 and TR1:

So going to check the various surrounding components but any pointers and hints is appreciated - As it has been so far from everyone in this thread.

Dillen
Top 10 Contributor
Copenhagen / Denmark
Posts 13,191
OFFLINE
Founder
Moderator
Dillen replied on Sun, Apr 11 2021 12:58 PM

Is the solenoid plunger broken?

Martin

kimhav
Top 500 Contributor
Malmo, Sweden
Posts 314
OFFLINE
Bronze Member
kimhav replied on Sun, Apr 11 2021 1:43 PM

No the solenoid plunger looks fine and moves smoothly when applying gentle movement to it. And to be mentioned I did use it for couple of hours last weekend before it stopped working once it was done playing a record; meaning moving the sledge back to 'parking' mode. Obviously something spiked in the PCB1. Currently I've replaced C2 (470uF), C28 (2.2uf) and D1 & D2 (1N 4002) including TR3-5 (BC337-35).

Checked the rest of the transistors which seems within expected measurement range when checking values between base and collector/emitter with exception for TR6 (92 PU51) which measured between base & collector (658) and base & emitter (301). So seems that TR6 needs to be replaced as well if this isn't the expected behaviour of this PNP transistor and that 92PU51 can be replaced by 2SA1593 or BD508.

kimhav
Top 500 Contributor
Malmo, Sweden
Posts 314
OFFLINE
Bronze Member
kimhav replied on Sun, Apr 11 2021 6:46 PM

Here is a guess for what to be looking at next; since TR6 seems to be a bit wonky I would assume that due to this that the motor might be drawing too much from the 5V which could potentially or most likely also blew D2 which is used to regulate the 5V for the most of the parts on this board based on that D1 was verified to be bad as well.

While I could test by removing D2 and test but don't really have and 12V to feed with, well could use a 9V battery plus some resistor to bring down to appropriate level to verify if it's working order. Could also remove TR6 and measure the 5V over D2 to see what it shows. Or I just go for replacing Tr6 and D2 and try then. What is your take on this?

Page 1 of 2 (47 items) 1 2 Next > | RSS